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Troubleshooting Process Plant Control
Other Books by Norman P. Lieberman

Copies of the first three texts are best ordered from the publishers, but may be ordered through us. E-mail (norm@lieberman-eng.com). Troubleshooting Refinery Operations (1980) has been incorporated into Troubleshooting Process Operations.

Troubleshooting Process Plant Control

A Practical Guide to Avoiding and Correcting Mistakes

Second Edition

Norman P. Lieberman

Process Improvement Engineering

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Dedication to Second Edition

Time goes on. And life goes on. The seasons progress from fall, to winter, into spring, same with me. I was young, then progressed to middle age. Became old. And then I peaked at age 74, and became younger again!

How did this happen?

My wife and inspiration, Liz, explained it to me, “Norm, you had a chance to retire 5 years ago. Now it's too late.”

I guess then I'll have to go on to the end, Liz and I together. Old Process Engineers never die; they just fade away.

March, 2017

Preface to the Second Edition

I have been practicing process engineering for 54 years. Mainly, as a refinery field troubleshooter for distillation operations, vacuum systems, fired heaters, compressors, and pumps. The majority of the malfunctions I discover are not due to faulty equipment design, mechanical failure, or operator error. The big problem is with process control.

I always explain during my process equipment troubleshooting seminars, which I've instructed since 1983 to over 20,500 attendees, that the Process Control Engineer is the most important person in the plant. I was sure of that in 1983, and am equally sure as I write these words in 2016.

The problem that the refining, petrochemical, and chemical fertilizer industry has is that the University course of study for process control engineers is worse than bad. It's irrelevant! In 1979 at Northwestern, and in 1983 at LSU, I found this out personally, having been ejected from both institutions after 1 day as an instructor. My conception of the training required to be an effective Process Control engineer, being at odds with that of both Universities.

Process control has little to do with math, or computers, or Laplace transforms. It's about understanding the following:

I wasn't particularly knowledgeable about process control until 1974, even though I had been employed by Amoco Oil for 10 years. But in 1974, I worked as an operator for 4 months, during a strike in Texas City. Then again in 1980, there was an even longer strike, part of which I worked as the panel operator on a sulfur recovery and amine unit. Afterward, I was fairly competent to tackle a variety of process control issues.

Based on my subsequent 36 years of experiences, I have developed the following advice for young Process Control Engineers:

“The price we pay for success is the willingness to risk failure.” Michael Jordan, Chicago Bulls.

You can email me with questions at norm@lieberman-eng.com

Introduction— Second Edition

Troubleshooting process plant control first requires an understanding of a wide variety of malfunctions that may develop in measuring variables such as:

Certainly, if you cannot measure a level or pressure, you can't expect to control it.

Second, the console operator or process engineer must understand how the control valves and the signals to open and close the valves actually work. For instance, did you know that the valve position shown in the control center does not at all represent the actual valve position? It represents what the control valve position is supposed to be.

To troubleshoot process control problems, the operator, or engineer, has to understand the relationship of the controls to the individual process. This means, you will have to get to know the unit and how it works. This is the most difficult part of the job of understanding process plant control.

Many apparent control problems are, in reality, process problems. But, on the other hand, after 53 years of troubleshooting refinery process problems, I am quite sure that the most common sort of malfunctions I have encountered are related to the inability to measure a level, temperature, or flow correctly—and also to have a control valve respond in the manner needed to achieve the desired operational change.

Auto Versus Manual

When you see that the console operator is running a control loop on “manual” rather than in “auto”, that is an indication that something is wrong with the field measurement of the variable, or with the control logic. Is it a metering problem, a sensor that is fouled, or a variable that is over-ranged? Perhaps, the variable is caught up in a “positive feedback loop”? Control loops are supposed to run in auto, and you should not accept loops that run in manual, as representing an acceptable mode of operation. Sooner or later, such broken (i.e., manual) control loops will slip out of an acceptable operating range.

Gain, Reset, and Advanced Computer Control

This text does not deal with the time aspects of optimizing the relationship between variables. Typically, the console operator is far less concerned about how fast operating parameter returns to its set point, than if a particular variable is moving in the right direction, so that he can safely bring his products back on spec.

Advanced computer control is largely irrelevant to my work in field troubleshooting refinery and petrochemical plant process control problems. I cannot conceive as to why process control engineering is so often taught in Universities as if it is a form of higher mathematics. Even more detrimental to unit operations is the perception by plant management and staff engineers that advanced computer controls are actually being utilized on the operating units, when in reality the console operators are struggling to run critical control loops on auto, without getting caught up in a dangerous positive feedback loop. I never understood anything about Laplace transforms in school, and I am certainly too old to start learning now.

About the Author

Norm Lieberman has been troubleshooting refinery and chemical plant process equipment since 1964. He began work at American Oil as a process engineer at their Indiana Refinery. Lieberman designed and operated sulfur plants, alkylation units, cokers, distillation towers, and vacuum systems for Amoco until 1980. He was next employed at the Good Hope Refinery in New Orleans where he worked on their polymerization unit, MTBE plant, crude unit, naphtha reformer, and hydrodesulfurization facilities.

In 1985 Lieberman worked for Good Hope, troubleshooting gas field compression, dehydration and treating problems for their Loredo, TX natural gas production facilities. In 1988, he became a consultant for petrochemical and refinery process equipment problems.

Approximately 20,500 engineers and technicians have attended his 850 in-house troubleshooting seminars. Lieberman has a degree in Chemical Engineering, 1964, from Cooper Union. He lives in New Orleans.

1
Learning from Experience

An old Jewish philosopher once said, “Ask me any question, and if I know the answer, I will answer it. And, if I don't know the answer, I'll answer it anyway.” Me too. I think I know the answer to all control questions. The only problem is, a lot of my answers are wrong,

I've learned to differentiate between wrong and right answers by trial and error. If the panel board operator persistently prefers to run a new control loop that I've designed in manual, if he switches out of auto whenever the flow becomes erratic, then I've designed a control strategy that's wrong. So, that's how I've learned to discriminate between a control loop that works and a control strategy best forgotten.

Here's something else I've learned. Direct from Dr. Shinsky, the world's expert on process control:

I've no formal training in process control and instrumentation. All I know is what Dr. Shinsky told me. And 54 years of experience in process plants has taught me that's all I need to know.

Learning From Plant Operators

My first assignment as a Process Engineer was on No. 12 Pipe Still in Whiting, Indiana. This was a crude distillation unit. My objective was to maximize production of gas oil, as shown in Figure 1-1. The gas oil had a product spec of not more than 500 ppm asphaltines. The lab required half a day to report sample results. However, every hour or two the outside operator brought in a bottle of gas oil for the panel board operator. The panel operator would adjust the wash oil flow, based on the color of the gas oil.

A schematic diagram representing oil plant, where wash oil, sample, colorimeter, and gas oil are labeled.

Figure 1-1 Adjusting wash oil based on gas oil color

While plant supervision monitored the lab asphaltine sample results, plant operators ignored this analysis. They adjusted the wash oil rate to obtain a clean-looking product. The operators consistently produced a gas oil product with 50–200 ppm asphaltines. They were using too much wash oil. And the more the wash oil used, the lower the gas oil production.

I mixed a few drops of crude tower bottoms in the gas oil to obtain a bottle of 500 ppm asphaltine material. I then instructed the panel board operators as follows:

The color of gas oil from a crude distillation unit correlates nicely with asphaltine content. The gas oil, when free of entrained asphaltines, is a pale yellow. So, it seems that my procedure should have worked. But it didn't. The operators persisted in drawing the sample every 1–2 hours.

So, I purchased an online colorimeter. The online colorimeter checked whether the gas oil color was above or below my set point. With an interval of 10 minutes, it would move the wash oil valve position by 1%. This never achieved the desired color, but the gas oil product was mixed in a tank. The main result was that gas oil production was maximized consistent with the 500 ppm asphaltine specification.

One might say that all I did was automate what the operators were already doing manually, that all I accomplished was marginally improving an existing control strategy by automating the strategy. But in 1965 I was very proud of my accomplishments. I had proved, as Dr. Shinsky said, “If it does work on manual, we can automate it.”

Learning From Field Observations

Forty-eight years ago I redesigned the polypropylene plant in El Dorado, Arkansas. I had never paid much attention to control valves. I had never really observed how they operate. But I had my opportunity to do so when the polypropylene plant was restarted.

The problem was that the purchased propylene feed valve was too large for normal service. I had designed this flow for a maximum of 1600 BSD, but the current flow was only 100 BSD. Control valve response is quite nonlinear. Nonlinear means that if the valve is open by 5%, you might get 20% of the flow. If you open the valve from 80 to 100%, the flow goes up by an additional 2%. Nonlinear response also means that you cannot precisely control a flow if the valve is mostly closed. With the flow only 20% of the design flow, the purchased propylene feed was erratic. This resulted in erratic reactor temperature and erratic viscosity of the polypropylene product.

The plant start-up had proceeded slowly. It was past midnight. The evening was hot, humid, and very dark. I went out to look at the propylene feed control valves. Most of the flow was coming from the refinery's own propylene supply. This valve was half open. But the purchased propylene feed valve was barely open. The valve position indicator, as best I could see with my flashlight, was bumping up and down against the “C” (closed) on the valve stem indicator.

The purchased propylene charge pump had a spillback line, as shown in Figure 1-2. I opened the spillback valve. The pump discharge pressure dropped, and the propylene feed valve opened to 30%. The control valve was now operating in its linear range.

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Figure 1-2 Opening spillback to keep FRC valve in its linear operating range

Now, when I design a control valve to handle a large reduction in flow, I include an automated spillback valve from pump discharge to suction. The spillback controls the pump discharge pressure to keep the FRC valve between 20 and 80% open. Whenever I sketch this control loop I recall that dark night in El Dorado. I also recall the value of learning even the most basic control principles by personal field observations.

Learning From Mistakes

Adolf Hitler did not always learn from his mistakes. For example, he once ordered a submarine to attack the Esso Lago Refinery in Aruba. The sub surfaced in the island's harbor and fired at the refinery. But the crew neglected to remove the sea cap on the gun's muzzle. The gun exploded and killed the crew.

I too had my problems in this refinery. The refinery flare was often very large and always erratic. The gas being burned in the flare was plant fuel. The plant fuel was primarily cracked gas from the delayed coker, supplemented (as shown in Fig. 1-3) by vaporized LPG. So much fuel gas was lost by flaring that 90% of the Aruba's LPG production had to be diverted to fuel, via the propane vaporizer.

A schematic diagram representing propylene charge pump, where propylene tank, spillback valve, FRC valve are depicted.

Figure 1-3 Unintentional flaring caused by malfunction of LPG makeup control valve is an example of split-range pressure control

I analyzed the problem based on the dynamics of the system. I modeled the refinery's fuel consumption versus cracked gas production as a function of time. The key problem, based on my computer system dynamic analysis, was the cyclic production of cracked gas from the delayed coker complex. My report to Mr. English, the General Director of the Aruba Refinery, concluded:

  1. The LPG vaporizer was responding too slowly to changes in cracked gas production from the delayed coker.
  2. The natural log of the system time constants of the coker and vaporizer was out of synchronization.
  3. A feed-forward, advanced computer control based on real-time dynamics would have to be developed to bring the coker vaporizer systems into dynamic real-time equilibrium.
  4. A team of outside consultants, experts in this technology, should be contracted to provide this computer technology.

Six months passed. The complex, feed-forward computer system was integrated into the LPG makeup and flaring controls shown in Figure 1-3. Adolf Hitler would have been more sympathetic than Mr. English. The refinery's flaring continued just as before. Now what?

Distressed, discouraged, and dismayed, I went out to look at the vaporizer. I looked at the vaporizer for many hours. After a while I noticed that the fuel gas system pressure was dropping. This happened every 3 hours and was caused by the cyclic operation of the delayed coker. This was normal.

The falling fuel gas pressure caused the instrument air signal to the LPG makeup valve to increase. This was an “Air-to-Open” valve (see Chapter 13), and more air pressure was needed to open the propane flow control valve. This was normal.

But, the valve position itself did not move. The valve was stuck in a closed position. This was not normal.

You will understand that the operator in the control room was seeing the LPG propane makeup valve opening as the fuel gas pressure dropped. But the panel board operator was not really seeing the valve position; he was only seeing the instrument air signal to the valve.

Suddenly, the valve jerked open. The propane whistled through the valve. The local level indication in the vaporizer surged up, as did the fuel gas pressure. The flare valve opened to relieve the excess plant fuel gas pressure and remained open until the vaporizer liquid level sank back down, which took well over an hour. This all reminded me of the sticky side door to my garage in New Orleans.

I sprayed the control valve stem with WD-40, stroked the valve up and down with air pressure a dozen times, and cleaned the stem until it glistened. The next time the delayed coker cycled, the flow of LPG slowly increased to catch the falling fuel gas pressure, but without overshooting the pressure set point and initiating flaring.

My mistake had been that I had assumed that the field instrumentation and control valves were working properly. I did not take into account the probability of a control valve malfunction. But at least I had learned from my mistake, which is more than you could say for Adolf Hitler.

Learning From Theory

Northwestern University has an excellent postgraduate chemical engineering program. I know this because I was ejected from their faculty. I had been hired to present a course to their graduate engineers majoring in process control. My lecture began:

“Ladies and gentlemen, the thing you need to know about control theory is that if you try to get some place too fast, it's hard to stop. Let's look at Figure 1-4. In particular, let's talk about tuning the reflux drum level control valve.

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Figure 1-4 Tuning a level control valve depends on what is downstream

Do I want to keep the level in the drum close to 50%, or doesn't it matter? As long as the level doesn't get high enough to entrain light naphtha into fuel gas, that's okay. What is not okay is to have an erratic flow feeding the light naphtha debutanizer tower.

On the other hand, if the overhead product was flowing into a large feed surge drum, than precise level control of the reflux drum is acceptable.

In order for the instrument technician to tune the level control valve, you have to show him what you want. To do this, put the level valve on manual. Next, manipulate the light naphtha flow to permit the level swings in the reflux drum you are willing to tolerate. But you will find that there is a problem. If you try to get back to the 50% level set point quickly, you will badly overshoot your level target.

If you return slowly to the set point, it's easy to reestablish the 50% level target. However, the level will be off the target for a long time.

In conclusion, ladies and gentlemen, tuning a control loop is a compromise between the speed at which we wish to return to the set point and our tolerance to overshooting the target. To establish the correct tuning criteria, the control loop is best run on manual for a few hours by the Process Control Engineer. Thank you. Class adjourned for today.”

My students unfortunately adjourned to Dean Gold's office. Dean Gold lectured me about the student's complaints.

“Mr. Lieberman, did you think you were teaching a junior high school science class or a postgraduate course in process control?”

And I said, “Oh! Is there a difference?”

So that's how I came to be ejected from the faculty of Northwestern University after my first day of teaching.

Learning From Relationships

My ex-girlfriend used to tell me, “Norm, the reason we get along so well is that I give you a lot of positive feedback.” From this I developed the impression that positive feedback is good. Which is true in a relationship with your girlfriend. But when involved in a relationship with a control loop, we want negative feedback. Control logic fails when in the positive feedback mode of control. For example:

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Figure 1-5 Too much steam flow causes a loss in vacuum

Many control loops are subject to slipping into a positive feedback loop. The only way out of this trap is to switch the controls to manual and slowly climb back out of the trap. Once you guess (but there is no way to know for sure) that you are in the safe, negative feedback mode of control, you can then safely switch back to automatic control.

Normal Purpose of Control Loops

Typically, a control loop is tuned to achieve two objectives:

  1. To return a variable to its set point as fast as possible.
  2. To avoid overshooting the set point.

If a heater outlet set point is at 700°F, and it's currently running at 680°F, the firing rate should increase. However, if the firing rate increases too fast, the heater outlet may jump past the set point to 720°F.

Tuning a control loop is meant to balance the instrument, “gain and reset,” to balance these two contradictory objectives.

The balance between gain and reset (i.e., instrument tuning) is not the main object of this text. Only rarely have I seen a panel board operator complain about this problem.

Another purpose of control is to optimize process variables. This is an advanced control that attempts to optimize certain variables. This is also not the sort of problem that the panel operator would be concerned about. An example of advanced control would be to optimize the ratios of several pumparounds, versus the top reflux rate, for a refinery crude distillation tower. For the units I work on, such advanced computer control is rarely used, or has been simplified, so that it is not much different than ordinary closed-loop control.

Manual Versus Auto

In reality, the main complaint about control loops that are communicated to me by operators is that the controller will not work in the automatic mode of control, and that the operators are forced to run the control loop in manual. This greatly increases and complicates their work.

To a large extent, this text examines why control loops are forced to run in the manual mode. A few of the reasons are the following:

  1. The control loop is trapped in a “positive feedback loop.” This is often a dangerous situation.
  2. There is no direct relationship between the variable being controlled and the response of the control valve. This is typically a design error.
  3. The facility that measures the process parameter in the field is not working correctly. This represents the majority of control problems that I have seen.
  4. The bypass valve is open around the control valve.
  5. The control valve is running too far closed because it is oversized, or badly eroded.
  6. The control valve is running too far open, because it is too small, or its port size is too small, or an isolation gate valve in the system is partly closed.
  7. The control valve's “Hand Jack” has been left engaged. Thus, the control valve cannot be manipulated from the computer console or panel. The hand jack is a mechanical device, used to manually move the control valve in the field.
  8. The control valve is stuck in a fixed position.
  9. The air signal connection to the diaphragm that moves the control valve has come loose.
  10. The diaphragm is leaking, so the sufficient instrument air pressure cannot be applied to the control valve mechanism to force it to move.

Process Control Nomenclature

The reader who is new to process plant vocabulary may wish to briefly skip to the glossary at the end of this book. I have assembled a list of “Process Control Nomenclature Used in Petroleum Refineries and Petrochemical Plants.” As in any other industry, your coworkers will have developed a vocabulary of their own, and will assume you understand the terms they employ. To an extent, in the following chapters of this text, I have also made a similar assumption.

A brief review of these terms may make it easier for you to communicate with some of your coworkers.